
Firstly, in regard to the post that I put up earlier about the blow-out preventer not working effectively, an early story noted that the BOP had recently been tested (thanks Gail).
Mr. Hayward said the blowout preventer was tested 10 days ago and worked. He said a valve must be partly closed, otherwise the spillage would be worse.
There are a number of things that can go wrong with a blowout preventer, said Greg McCormack, director of the Petroleum Extension Service at the University of Texas, which provides training for the industry.
The pressure of the oil coming from below might be so great that the valves cannot make an adequate seal. Or in the case of a shear ram, which is designed to cut through the drill pipe itself and seal it off, it might have encountered a tool joint, the thicker, threaded area where two lengths of drilling pipe are joined.
Still, Mr. McCormack said, “something is working there because you wouldn’t have such a relatively small flow of oil.” If the blowout preventer were completely inoperable, he said, the flow would be “orders of magnitude” greater.
However oil is now flowing through the BOP and out into the water immediately above the well site on the sea bed. When the site was visited by a small remotely operated vehicle with cameras they showed(see below) that the riser, the pipe that normally carries the oil from the sea bed to the surface, had kinked over when the rig sank, and oil was coming from three places:
The Coast Guard said it had not detected oil coming from the well Friday and assumed post-accident efforts to activate the blowout preventer “a huge stack of valves sitting atop the wellhead on the sea floor” had been successful.
But later trips by the remotely operated vehicles (ROV’s), discovered oil shooting from the end of the pipe-like riser that had connected the rig to the blowout preventer.
A second, smaller leak was found in a section of drill pipe near the wellhead.
That 21-inch-diameter riser had become detached from the rig when it sank. In the process, it was folded over at a 90-degree angle just above the wellhead, which had the effect of kinking it like a garden hose and constraining the flow of oil from the well. It now sits in a long, meandering mess on the ocean bottom. This helps explains why oil was not initially thought to be seeping.” . . . . . . The preferred option, he said, is still to find a way to engage the blowout preventer. That fix, if it works, could be handled in a matter of days, he said.
But if that doesn't work, the other option is to drill a deep “relief” well into the damaged well and stem the flow of oil, though that option could take several months, Suttles acknowledged. He said his team would spend the next several days trying to determine the best method.
The problem lies, in part, with the capabilities of the ROV’s and their ability to get access to the well site on the sea-bed.
There is a report from a survivor (h/t Fractional Flow) that says that the well was shut in and they were going through the process of separating the rig from the well, and moving it off. They began by cleaning out the drilling mud from the riser, replacing it with sea water. However, when they re-opened the valves at the top of the well, the pipe in the well had become filled with gas from the well, under considerable pressure, and this “Kicked” the well as the valve opened. Gas, as the pressure gets less as it moves up the pipe, expands much more than oil. And unfortunately in the process of disconnection, the pressure to hold the gas, which comes from the density of the drilling mud in the riser initially, had been removed as part of the disconnection process.
So the high pressure gas was able to blow all the sea water in the riser out onto the deck of the rig. (This happens extremely quickly, well below a minute) The gas then followed, and as it flowed out of the pipe at the top of the well there was some hot source that caused it to ignite. (This could even be from a static electricity spark). Because of the depth of the well, the pressure in the bottom of the well was in the 30-40,000 psi range.
Part of the problem that arises with flows at that pressure is that any abrasive particles (such as small pieces of rock) will cut through metal at the speeds at which it is carried. (Such jets were used to remove the damaged tops of the wells in Kuwait after the Gulf War, for example). So that it is possible that as the BOP started to function the high-velocity flow may have eroded part of the system to allow some fluid to bypass the plug that the BOP inserted. If that happened then the continued flow would just enlarge the passage again fairly quickly, so that the BOP will become ineffective.
However there are pictures of the leaks available.

At this stage there does not appear to be that great a driving pressure for the oil coming out of the well. (If there were the flow would be more directed horizontally) This suggests that the BOP did at least partially function, and that the passage may have been eroded by the particles in the gas and oil now escaping.
There is a recent report that the accident may have been caused by a poor cementing job by Haliburton:
After an exploration well is drilled, cement slurry is pumped through a steel pipe or casing and out through a check valve at the bottom of the casing. It then travels up the outside of the pipe, sheathing the part of the pipe surrounded by the oil and gas zone. When the cement hardens, it is supposed to prevent oil or gas from leaking into adjacent zones along the pipe.However it is hard to see from what is known, that this was a cause in this case.
As the cement sets, the check valve at the end of the casing prevents any material from flowing back up the pipe. The zone is thus isolated until the company is ready to start production.
The process is tricky. A 2007 study by the U.S. Minerals Management Service found that cementing was the single most-important factor in 18 of 39 well blowouts in the Gulf of Mexico over a 14-year period. (But) . . . .
But at the time of the accident, "well operations had not yet reached the point requiring the placement of the final cement plug, which would enable the planned temporary abandonment of the well," the Halliburton statement said.
Interesting that the survivor calling in to Mark Levin said that the BOP stack had just been tested, whereas BP's CEO said it had been tested 10 days earlier. Big lawsuits grow from small discrepancies!
ReplyDeleteThe odd part in the survivor's testimony is that they took a kick immediately after circulating the riser over to seawater & opening the valves on the BOP stack. This suggests that the gas bubble was already sitting below the valve, having migrated there during the 16 hours or so since the cement job. The pressure below the value would thus have been abnormally high.
Opening a valve can be quite difficult when there is a high pressure differential across it -- something which has saved many of us from embarrassing mistakes. Surely it would be standard practice to check the pressure below the BOP stack before opening the valves?
I am not sure, Congressional hearings etc or whatever not withstanding, that we are now likely to ever know what really happened. The relevant equipment and records are now at the bottom of the Gulf, and sadly those most involved may have died.
ReplyDeleteBut if they thought that the well was plugged at the bottom then they might not have been that concerned. But there now seems to be a bit more debate over how far from finished Haliburton was.
I do like ur article~!!!...................................................
ReplyDeleteThere's one simple question I can't seem to find an answer to...
ReplyDeleteHow high can the pressure reach in a well like this? (in PSI)
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